About time for an update.....
Been a busy few months with the arrival of our little girl so sadly the LCR took a back seat a bit but I've not fallen off the wagon and got chance to spend the Saturday sorting out some the the "niggles" which I had kept getting put off previously.
Intercooler
Had my Forge FMIC fitted for almost a year now and was never totally happy with the fittment of the hoses as they seemed to twist slightly which eneded with one big twist when fitted to the charge pipe and caused the hose to rub against one of the coolant hoses...and well you can work out the rest!
Whilst i had the bumber off thought it would be rude not to give the FMIC a good clean and slap some autosol on and even went as far as blasting the insides with the jet wash to remove the oil residue inside.
BEFORE
AFTER
The only down side with trimming the pipes to fit snug was that it ment I lost the nice gap i had for my 4 inch CAF but thats a job for another day....
N249
Whilst i had previously relocated this (pipes and all) to the passenger wing a boost fault brought it back out of hibernation to eliminate the poissiblity that this was the issue and it never made it back.
This time round thought I got shot of all of the pipework totaly and made up a pair of wires using spade crimps to connect to the terminals rather the utilising the exisiting plug.
Found a nice new cubby hole just below the passenger headlight and looks so much neater IMO.
BEFORE
AFTER
I also seemed to be suffering intermittent boosting
problem where the car seem to be getting pushed into limp mode, although the boost gauge showed it was still boosting normally......

, so i decided to remove the ECS N75 I had fitted and go back to the standard DV location rather than using the relocation kit.
As of now I have done 100+ miles and all is holding up just fine.....fingers crossed!