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Was that Stealth? assume they sorted the car for you?
Cheaper than the £2500 they quoted for replacing the turbo!i want a new s3 but i am not jealous honest
that it was, and yes they did. Managed to sort in 20 minutes what SEAT couldn't sort out in an 8 hour day. I think they forgot to open the bonnet!Cheaper than the £2500 they quoted for replacing the turbo!
![Furious [:@] [:@]](/forums/styles/seatcupra/oldforumsmileys/furious.gif)
Well folks, it's time for todays instalment of 'what the bloody heck is wrong with this German/Spanish bastid car'
Driving home from work, pulled away from a junction with a nice open road in front of me.... In second gear, put my foot down, off she goes... oh, no, she doesn't. It felt normal for a second or two, revs flew up, speed rose nicely, grin on face got bigger.... and then it was as if something physical stopped all that. Imagine sucking through a straw and then having 95% of the end covered up. That's what it felt like.
From then on it stayed like that, and felt as if something physical was stopping me from making the normal power. Even the throttle felt different to depress.
Now somebody please correct me if I'm wrong, but a MAF or N75 wouldn't do that, would it? It would work... or not work. It wouldn't work and then pack up all of a sudden, would it?
And again, correct me if I'm wrong, but does this not yet again point towards a split hose somewhere? It's almost as if there was a sudden drop in pressure somewhere.
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could be a loose pipe, what i mean is when the engine gets hotter the pipes will expand and maybe cause a slight boost leak or vaccum leak
Turns out the MAF was giving some really erratic readings, but not all the time. As I understood it, the main cause of the problem was when the car was warm, under a constant load (i.e. cruising) and you put your foot down to accelerate. That ties in perfectly with what I had experienced!
And it made a whopping 165-ish-BHP!
