On one of the runs we logged even though throttle was 100% down, the plate closed to 40% briefly. Not sure if that was the ECUs last ditch attempt at cutting boost or something?!?!?
Its a K03S yeah.
Modifications are:
Forge Motor sport front mounted intercooler
Forge Motor sport turbo intake pipe
Forge Motor sport diverter valve (yellow spring)
Green cotton air filter element
Denso Iridium IK22 spark plugs (0.8mm gap)
Milltek Hi flow sports cat and downpipe (2 ½ inch)
Milltek full cat back exhaust system (2 ½ inch)
Spec Stage 2 clutch
Peloquin LSD
The map was done by CC.
Could it be a faulty N75? (I have no idea to be honest!!!)
Doubt it's the N75. You can see the ECU pulling the load back in 003.
A log of 114 would be interesting.......
Have you mentioned the problem to CC?

